summaryrefslogtreecommitdiff
diff options
context:
space:
mode:
authorjohn stultz <johnstul@us.ibm.com>2006-12-08 02:36:02 -0800
committerLinus Torvalds <torvalds@woody.osdl.org>2006-12-08 08:28:37 -0800
commit562f9c574e0707f9159a729ea41faf53b221cd30 (patch)
tree54fb7d5195d09cd7ce9ceb312a98d7538e8a34f0
parenta2ee8649ba6d71416712e798276bf7c40b64e6e5 (diff)
downloadlinux-3.10-562f9c574e0707f9159a729ea41faf53b221cd30.tar.gz
linux-3.10-562f9c574e0707f9159a729ea41faf53b221cd30.tar.bz2
linux-3.10-562f9c574e0707f9159a729ea41faf53b221cd30.zip
[PATCH] time: re-add verify_pmtmr_rate
This patch re-adds the verify_pmtmr_rate functionality from 2.6.17 that I dropped 2.6.18. This resolves problems seen on older K6 ASUS boards where the ACPI PM timer runs too fast. See: https://bugzilla.redhat.com/bugzilla/show_bug.cgi?id=211902 http://bugme.osdl.org/show_bug.cgi?id=2375 Thanks to Ian Campbell for re-reporting this and testing the fix! Signed-off-by: John Stultz <johnstul@us.ibm.com> Cc: Andi Kleen <ak@suse.de> Cc: Ian Campbell <ijc@hellion.org.uk> Cc: Ingo Molnar <mingo@elte.hu> Cc: Thomas Gleixner <tglx@linutronix.de> Cc: Roman Zippel <zippel@linux-m68k.org> Signed-off-by: Andrew Morton <akpm@osdl.org> Signed-off-by: Linus Torvalds <torvalds@osdl.org>
-rw-r--r--drivers/clocksource/acpi_pm.c36
1 files changed, 36 insertions, 0 deletions
diff --git a/drivers/clocksource/acpi_pm.c b/drivers/clocksource/acpi_pm.c
index 7fcb77a9d01..8ab61ef97b4 100644
--- a/drivers/clocksource/acpi_pm.c
+++ b/drivers/clocksource/acpi_pm.c
@@ -142,6 +142,39 @@ DECLARE_PCI_FIXUP_EARLY(PCI_VENDOR_ID_SERVERWORKS, PCI_DEVICE_ID_SERVERWORKS_LE,
acpi_pm_check_graylist);
#endif
+#ifndef CONFIG_X86_64
+#include "mach_timer.h"
+#define PMTMR_EXPECTED_RATE \
+ ((CALIBRATE_LATCH * (PMTMR_TICKS_PER_SEC >> 10)) / (CLOCK_TICK_RATE>>10))
+/*
+ * Some boards have the PMTMR running way too fast. We check
+ * the PMTMR rate against PIT channel 2 to catch these cases.
+ */
+static int verify_pmtmr_rate(void)
+{
+ u32 value1, value2;
+ unsigned long count, delta;
+
+ mach_prepare_counter();
+ value1 = read_pmtmr();
+ mach_countup(&count);
+ value2 = read_pmtmr();
+ delta = (value2 - value1) & ACPI_PM_MASK;
+
+ /* Check that the PMTMR delta is within 5% of what we expect */
+ if (delta < (PMTMR_EXPECTED_RATE * 19) / 20 ||
+ delta > (PMTMR_EXPECTED_RATE * 21) / 20) {
+ printk(KERN_INFO "PM-Timer running at invalid rate: %lu%% "
+ "of normal - aborting.\n",
+ 100UL * delta / PMTMR_EXPECTED_RATE);
+ return -1;
+ }
+
+ return 0;
+}
+#else
+#define verify_pmtmr_rate() (0)
+#endif
static int __init init_acpi_pm_clocksource(void)
{
@@ -173,6 +206,9 @@ static int __init init_acpi_pm_clocksource(void)
return -ENODEV;
pm_good:
+ if (verify_pmtmr_rate() != 0)
+ return -ENODEV;
+
return clocksource_register(&clocksource_acpi_pm);
}